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Home > News > India News > Article > Lack of pressure may have led to Chandrayaan 2 mission abortion

Lack of pressure may have led to Chandrayaan-2 mission abortion

Updated on: 16 July,2019 12:00 AM IST  | 
mid-day online desk |

The rocket Geosynchronous Satellite Launch Vehicle-Mark III GSLV-Mk III was supposed to lift off at 2.51 a.m. on Monday with India-s second moon mission spacecraft Chandrayaan-2

Lack of pressure may have led to Chandrayaan-2 mission abortion

A view of the Chandrayaan-2 on board GSLVMkIII-M1 at Satish Dhawan Space Centre in Nellore district, Saturday, July 13, 2019. Chandrayaan 2 suffered a jolt in the early hours of July 15 after a technical snag forced the Indian Space Research Organisation

Chennai: Two retired official of Indian space organisation said that non-building of sufficient pressure in the helium tanks in the -Bahubali- rocket could be the reason for calling off the moon landing mission Chandrayaan-2 one hour before the rocket-s take off.


The rocket Geosynchronous Satellite Launch Vehicle-Mark III GSLV-Mk III was supposed to lift off at 2.51 a.m. on Monday with India-s second moon mission spacecraft Chandrayaan-2.


"A technical snag was observed in launch vehicle system one hour before the launch. As a measure of abundant precaution, Chandrayaan2 launch has been called off for today. Revised launch date will be announced later," ISRO tweeted and didn-t elaborate further.


Retired officials of Indian Space Research Organisation ISRO said that there should be proper pressure in the liquid fuel tanks so that there is a continuous flow of fuel to the combustion chamber. A retired ISRO official said, "While the fuel is fed into the combustion chamber from the bottom, helium gas is filled from the top. It seems sufficient pressure was not being built up and hence the launch was called off." According to him, the flow of fuel to the combustion chamber should be uniform for the rocket to fly.

In 2006, the GSLV-F02 a different variant of GSLV went out of control less than a minute after lift-off and had to be destroyed in the air after it started breaking up. The reason for the failure, an expert committee in its failure analysis report said, was that a propellant regulator in one of the four strap-on liquid motors had much higher discharge coefficient in its closed condition.

"The reason for this could be an inadvertent error in manufacturing, which escaped the subsequent inspection, and acceptance test procedures. This regulator has functioned satisfactorily in all the previous 50 engines manufactured and tested so far," the report said.

"The primary cause for the failure was the sudden loss of thrust in one out of the four liquid propellant strap-on stages S4 immediately after lift-off at 0.2 sec. With only three strap-on stages working, there was a significant reduction in the control capability," the report said.

"However the vehicle attitude could be controlled till about 50 sec. At the same time the vehicle reached the transonic regime of flight and the vehicle attitude errors built up to large values, resulting in aerodynamic loads exceeding the design limits thus leading to break up of the vehicle," the report added.

According to that report, the thrust of the liquid engines used in the strap-on stages is precisely controlled by a set of regulators.

"Detailed analyses have indicated that in S4 engine the thrust control was not effective. Instead of stabilising at 5.85 MPa Mega Pascal chamber pressure, it reached 7.11 MPa at 2.8 sec. This was much beyond the design limits and the engine failed at 0.2 sec after lift-off, that is 5 sec after its ignition," the report said.

"The larger flow of propellant led to higher operating pressure in the gas generator 4.7 MPa against design specification of 3.6 MPa. Due to this higher operating pressure of the gas generator, the water flow rate into it got reduced. The combined effect of larger flow of propellants and reduced flow of water led to a very high gas temperature of 1,823 K against design specification of 900 K and pressure of 4.7 MPa against the design specification of 3.6 MPa.

"The very high operating pressure and temperature resulted in the structural failure of the gas generator. The consequent abrupt stopping of the turbo pumps that feed propellants at very high pressures to the engines led to loss of thrust of S4 engine.

"The water calibration tests conducted simulating the malfunction of the propellant regulator hardware could closely reproduce the flight phenomenon thereby confirming the larger flow area," the report said.

At that time ISRO ruled out any sabotage theories and said the quality checks and inspections has been strengthened. Incidentally, even the very first flight of GSLV slated for 28.3.2001 was automatically aborted seconds before the lift-off.

That launch was aborted with the automatic shutdown of the main engine just a second before the lift off. That too after the four liquid propulsion strap-on boosters started burning. The automatic shut off system was activated when it sensed that one of the strap-on boosters did not develop the required thrust. The vehicle was immediately disarmed. The rocket was later flown on 18.1.2001 carrying GSAT-1 satellite.

Edited by mid-day online desk with inputs from IANS

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